• This community needs YOUR help today!

    With the ever-increasing fees of maintaining our vibrant community (servers, software, domains, email), we need help.
    We need more Supporting Members today.

    Please invest back into this community to help spread our love and knowledge of all aspects of IH Cub Cadet and other garden tractors.

    Why Join?

    • Exclusive Access: Gain entry to private forums.
    • Special Perks: Enjoy enhanced account features that enrich your experience, including the ability to disable ads.
    • Free Gifts: Sign up annually and receive exclusive IH Cub Cadet Tractor Forum decals directly to your door!

    This is your chance to make a difference. Become a Supporting Member today:

    Upgrade Now

K321 Rebuild

IH Cub Cadet Forum

Help Support IH Cub Cadet Forum:

This site may earn a commission from merchant affiliate links, including eBay, Amazon, and others.

rfunk

Well-known member
Joined
Jun 14, 2019
Messages
187
Location
Winkler, Manitoba, Canada
displayname
Reynold Funk
Took my engine to an old-timer machinist recommended by local garden/lawn tractor shop. Ordered piston as advised, brought to him and had him fit it to the bored and honed cylinder. He also lapped the connecting rod mating surface a couple thou', as it was out-of-round vertically, but on-spec horizontally. I do recall an old engineering prof "engine guy" mentioning doing this. Anyone here heard of it, and, if so, what is your experience with doing this?
During reassembly, (hadn't really gotten around to cleaning up parts properly, before), I saw this:
IMG_20200516_141028075.jpg

Cracking?? around spark plug hole. Does not seem to go through head. Is this just a casting defect, or should I be ordering a new head?
I had intended to replace the balance gears, changed my mind after Digger gave me a call, but the shim washers he sent me came in handy anyway: they're the right size for adjusting the camshaft endplay, too. :greenthumb::greenthumb:
Made sure I checked the ring end gaps, too, my machinist repeated that lots . . .
Planned on doing the Dave Kamp mod on my driveshaft, went from PO's massacre:
IMG_20200330_220651148.jpg

to this:
IMG_20200519_183646074.jpg
IMG_20200519_183655367.jpg

Machine shop said it was easier just to make a new adapter. They'd made it just a bit oversize to go into the drive cup, so chucked the shaft end into my drill press, and gave it a couple light swipes with a file while turning. PERFECT!
IMG_20200519_210517462.jpg

Had the machine shop cross-drill the yokes, too, then used the yoke hole to line up and drill the shaft.
IMG_20200519_210932155.jpg

Yeah, much larger yokes than I'd like. Doesn't leave much room for the cooling fan. (to be ordered).

Last point of note, the old machinist showed me a crack in the deck, which he said shouldn't be an issue, as it was not up to the valve insert:
IMG_20200505_222524801.jpg

Again, comments/experience?

I've had to reassemble my engine with these known defects, because it's my WORKER. After I gave it a 10 minute run-in, I changed the oil and re-torqued the head bolts, then mowed for a couple hours. Not exactly what I'd like to have done, but noted "no" oil used, where before I rebuilt it, I'd have been down more than half a quart, and had the breather slimed up with oil drool. Hoping it stays together, don't want to waste the effort, but figured if the head lets go, at least that is an easy replacement.
Things I'd do differently if I did it again, may do yet, would be adding a larger air filter with an extension, based on the old machinist's comments that the very sandy ("potato growing") soil in my area tends to wear out Kohlers faster than more clayey soils in other, nearby areas. I'd also do some painting and other cleanup, but the grass just won't hold off that long. Maybe next year . . . sigh.
 
The cracks in the head and block wouldn't bother me too much as long as they don't grow. I would have replaced the original connecting rod if I was in the engine that far. I'm curious to hear how long the U-joint lasts in the driveshaft. Over the years, several people have done that, and not all have had good results.
 
The head would worry me enough to find a replacement. I don't think I'd swap it right away but more likely keep it on hand and replace it in the winter ( since this is a worker). The block wouldn't bother me at all. I'm also interested in your driveshaft "update", I've considered doing this to my 169 but I'm not convinced it's the way to go. So let us know how it's working out .
 
Thanks for the input, Matt and Mike. That's what I was hoping for.

The oversize u-joint itself should be ok, though I do have some concern over that much mass on the driveshaft. If I did it with more time, I would consider a 3/4" or 7/8" holllow shaft between the front and the back, to resist flexing better. That being said, the input shaft end was already a half-diameter or more off-center because of the wear, so a major improvement in balance of rotating mass. Looking at it during the first, 10 minute run-in, I noticed no visible shaft vibration at 3600 rpm, or at varying speeds less than that. It is a full, needle-bearing u-joint, not like some smaller ones I've seen with bushings only, and has a grease fitting.

I was concerned about how much vibration I would get from removing the balance gears, guess I lucked out on that, not very noticeable. I would consider the corrective added weight if I have to go into this engine again; I also want to contact a relative who has a custom machining company with a fair bit of automated equipment, but also himself and another guy who do the "special" jobs that need a master machinist's touch. He might be able to do the balance gears in steel, changing the design to a wider bearing spacing, instead of that 3/8" spacer on the shaft, at a reasonable price.

On the cracks, I'm planning on keeping an eye out for fire-breathing from under the top tin - I frequently find myself mowing into the evening, so lifting the hood while I idle it down after mowing, while blowing out the grass, should let me see if there's any through-cracking. It would probably also make itself very clear in the running and power, I imagine! I'm going to keep my eye out for a swapper or parts engine, they sometimes come up around here. (in the last year, I've seen: 16 hp K341 for $400 used, should have bought it, 12hp for $40, unknown condition, NEW K321 shortblocks, unknown price, currently advertised as of 2020 05 28).
 
Thanks, David. I've "stolen" one of his other ideas, already. Drilled a hole into the drain plug and used high-temp epoxy to fasten in a high-strength magnet. Amazing how much metal dust gets created in just the 10 minutes of breaking it in.
 
The cracks in the head and block wouldn't bother me too much as long as they don't grow. I would have replaced the original connecting rod if I was in the engine that far. I'm curious to hear how long the U-joint lasts in the driveshaft. Over the years, several people have done that, and not all have had good results.
I put ujoints in my 147 20 years ago and have had wonderful luck, still on the same ones!
 
FWIW

Forget the balance gears and ad Dave Kirks balance plate instead.
The K341 I did over the winter has the plate and it is the smoothest running Cub I have.


And my experience is the exact opposite! I would never do it again! I'm glad I kept all the old parts. If I can find the bearings and journals I am putting the gears back in.
 
So, I've got an update. My 149 has been increasingly hard to start. Finally noticed that the crack in the head was puffing, most noticeable cold, but also blowing oil onto the plug. I've been trying to source one locally, should've bought one last year, local guy was selling out his dad's estate, would have been $200 Canadian. Talking with my neighbour yesterday about something else, he mentioned that he had an old Kohler auger motor on his junk pile he'd switched out because it was hard to start, but he thought it would be too small. 50 yards walk proved it to be exactly what I needed the head from - just the later model with starter and stator charging. He even delivered with his tractor bucket. SCORE!!! About the driveshaft mods, still looking good. Three years, about 60 hours (aftermarket Hobbs meter has proved unreliable)
The auger motor actually even cranked when I put a battery on it . . .
 
I put ujoints in my 147 20 years ago and have had wonderful luck, still on the same ones!
If you look at the late 70 early eighties ford lgt 165 and 145's , they have a ujoint assembly in them factory.
 
I have a question for you all, my 147 which has been sitting for over a year now has a crack in it's block (k321) and I have been under the impression that it would need to be replaced. However the crack does not reach a valve nor the cylinder, or at least it didn't when I last saw it. Would it actually be okay to run? I consider the old trick of drilling a small hole into the end of the crack as a method to prevent it from growing, would that be helpful?
 
My GUESS would be, if it doesn't go into the cylinder or the ports, and doesn't seem to impact structural integrity, go ahead and run it. It might be a casting defect that may only cause trouble 20 years from now. Yes, it could fail the day after you put it together, but cost/risk/benefit analysis should be able to let you make an informed decision.
 
So, I've got an update. My 149 has been increasingly hard to start. Finally noticed that the crack in the head was puffing, most noticeable cold, but also blowing oil onto the plug. I've been trying to source one locally, should've bought one last year, local guy was selling out his dad's estate, would have been $200 Canadian. Talking with my neighbour yesterday about something else, he mentioned that he had an old Kohler auger motor on his junk pile he'd switched out because it was hard to start, but he thought it would be too small. 50 yards walk proved it to be exactly what I needed the head from - just the later model with starter and stator charging. He even delivered with his tractor bucket. SCORE!!! About the driveshaft mods, still looking good. Three years, about 60 hours (aftermarket Hobbs meter has proved unreliable)
The auger motor actually even cranked when I put a battery on it . . .
Update: got the donor head sanded flat, installed. It fired up first time over, hasn't done that in a long time. That crack must have been killing vacuum (thus mixture in) for quite a while. Now I just need to tap the stud holes in the block, as the threads in the exhaust port are gone . . .
 
Update question: the exhaust port threads are gone. The exhaust elbow will not stay in place. Has anyone cleaned out and tapped the holes beside the exhaust port for bolts or studs? Is it realistic?
 
The holes may already be threaded. The ones in my 1450 were. I had the same issue, the “lock nut” had vibrated loose on the PO… (easn’t the only thing I had to fix, it took ISO mounts, cradle mod and an oil pan it, it had rattled around so much. The wire cleaner cover was actually rubbing the side panel) and walleyed out the threads. A buddy made a flange for me, that was maybe a 1/2 inch thick, threaded for the elbow (1 inch pipe, if I remember correctly) and 2 holes drilled to patch the bolt holes. IT is basically the “lemon shape” of Kohler carb gasket. Most gasket kits have that gasket in it….. It’s not the best solution, but has worked for several years, and this is one of my workhorses….
 
The holes may already be threaded. The ones in my 1450 were. I had the same issue, the “lock nut” had vibrated loose on the PO… (easn’t the only thing I had to fix, it took ISO mounts, cradle mod and an oil pan it, it had rattled around so much. The wire cleaner cover was actually rubbing the side panel) and walleyed out the threads. A buddy made a flange for me, that was maybe a 1/2 inch thick, threaded for the elbow (1 inch pipe, if I remember correctly) and 2 holes drilled to patch the bolt holes. IT is basically the “lemon shape” of Kohler carb gasket. Most gasket kits have that gasket in it….. It’s not the best solution, but has worked for several years, and this is one of my workhorses….
I wish . . . the holes are really rusty, so even if they were threaded originally, the threads are gone. I'll have to remove the rust before I can even try a drill bit. Going to be a bit of an experiment.
 
Checked the holes with a bright light, there were threads there at one point. Damaged and rusted now. I'll have to move the muffler to see if threading the port deeper might work.
 
So, further examination, muffler off, the threads in the block are good, it's the threads on the exhaust elbow that gave out. Before I bite the bullet and order a new $$ elbow, would it be worth cutting off the worn-out threads and seeing if the elbow will thread in tightly? Maybe nothing to lose? If that doesn't work, try welding on a 1" pipe nipple? Opinions, ideas?
 

Attachments

  • 20240525_131438.jpg
    20240525_131438.jpg
    2.7 MB
  • 20240525_131413.jpg
    20240525_131413.jpg
    2.7 MB
So, further examination, muffler off, the threads in the block are good, it's the threads on the exhaust elbow that gave out. Before I bite the bullet and order a new $$ elbow, would it be worth cutting off the worn-out threads and seeing if the elbow will thread in tightly? Maybe nothing to lose? If that doesn't work, try welding on a 1" pipe nipple? Opinions, ideas?
I's cut off a short nipple and weld on the elbow you now have.
I have done that several times w/good results.

Here's how,
Get a 6" or so 1" black nipple w/thread on both ends and a 1"coupling.
Screw what you can of the old elbow into one end of the coupling and the new nipple into the other end. mount this ***'y in a band saw holding it by the nipple so your cut off if the old threaded part of the elbow will be square. Cut a bit beyond where the old threads stop so you will have room to weld the new part on w/o screwing up the threads.

Figure out how long a piece of new threaded mat'l you will need to cut from the nipple.
Do not make it too long or too short as you need to be sure and clear the governor arm when it's screwed into the block.
 

Latest posts

Back
Top