klindstedt
Well-known member
Time for an update on the 109 that followed me home a few weeks ago. Or should I say *129*
Harry was correct, the engine had been replaced at sometime with a K301 12hp engine. Well... I first worked on tracking down the no-start problem. Turns out that the metal tab that presses on the neutral start safety switch was missing. By jumping out that switch I was able to confirm the S/G would turn over. I removed the gas tank and filled with acetone to cut the old gas 'gunk', rebuilt the carb, replaced the fuel lines and filter. With a splash of fresh gas, I got it to start, but only by jumping the battery from my truck and spraying a little starting fluid in the intake. It was running a little rough at first, but settled into a fairly smooth idle. I walked away from the shed and when I came back it had died. This time I got nothing when I turned the key. checked my jumper and it was fine. Had to get ready for church and closed the door on it for the day.
The next day I pushed it into my garage where I have more room and better light and started tracking down the electrical problem again. Finally tracked it down to a flaky, intermittent ignition switch. I jumpered the BAT terminal to IGN and then jumped the S/G and got it to start again. I took it out in the yard and did a few mowing rounds on the lawn. It was making some noise - not exactly a backfire, but could have been. The noise was getting worse, so I brought it up by the garage to fiddle with the carb settings thinking I had it too lean or too rich. Before I could make any changes I noticed it was REALLY hot, like smoking. I shut it down (hopefully) before damaging anything.
That evening I did a little research on the forum for similar problems and decided it wouldn't hurt anything to replace the plug, points, and condenser. I replaced the coil as well because I found it had a crack around the tower that was 'sealed' with caulk.
I replaced all those items, set the point gap at .020, checked that the valve clearances were set at .008 (intake) and .018 (exhaust), which they were close to, just adjusted the intake a little. Tried to start it again and had to jump it again. The starter generator doesn't seem to have enough 'oomph' to turn it over very fast. Got it started, but no great improvement in how it is running.
Wondering now if the ACR is not working and the S/G is struggling against the compression. I also have a new head gasket and I'm going to remove the head to de-carbon and check the exhaust valve movement at that time. Might also try static timing the engine rather than using the .020 setting on the points.
Anything else I should be looking at? Oh, forgot to mention that the air cleaner cover and base were all covered in a black sooty film as I received it from the previous owner and when the tractor was overheating I could see gasses blowing out the air cleaner every so often.
Thanks
The next day I pushed it into my garage where I have more room and better light and started tracking down the electrical problem again. Finally tracked it down to a flaky, intermittent ignition switch. I jumpered the BAT terminal to IGN and then jumped the S/G and got it to start again. I took it out in the yard and did a few mowing rounds on the lawn. It was making some noise - not exactly a backfire, but could have been. The noise was getting worse, so I brought it up by the garage to fiddle with the carb settings thinking I had it too lean or too rich. Before I could make any changes I noticed it was REALLY hot, like smoking. I shut it down (hopefully) before damaging anything.
That evening I did a little research on the forum for similar problems and decided it wouldn't hurt anything to replace the plug, points, and condenser. I replaced the coil as well because I found it had a crack around the tower that was 'sealed' with caulk.
I replaced all those items, set the point gap at .020, checked that the valve clearances were set at .008 (intake) and .018 (exhaust), which they were close to, just adjusted the intake a little. Tried to start it again and had to jump it again. The starter generator doesn't seem to have enough 'oomph' to turn it over very fast. Got it started, but no great improvement in how it is running.
Wondering now if the ACR is not working and the S/G is struggling against the compression. I also have a new head gasket and I'm going to remove the head to de-carbon and check the exhaust valve movement at that time. Might also try static timing the engine rather than using the .020 setting on the points.
Anything else I should be looking at? Oh, forgot to mention that the air cleaner cover and base were all covered in a black sooty film as I received it from the previous owner and when the tractor was overheating I could see gasses blowing out the air cleaner every so often.
Thanks